Transwestern Pipeline Company Notice 115365

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Notice Type Description: Force Majeure
Notice Identifier: 115365
Critical Notice Description: Critical notice
Posting Date/Time: Feb 25 2026 9:30AM
Notice Status Description: Supersede
Required Response Indicator Description: No response required
Response Date/Time:
TSP: 7933047
TSP Name: TRANSWESTERN PIPELINE COMPANY, LLC
Subject: Force Majeure - Compressor Station P3 - 2/22/2026 (Intraday 3) through 3/05/2026 Revision 1
Notice Effective Date/Time: Feb 22 2026 4:50PM
Notice End Date/Time: Mar 6 2026 8:59AM
Notice Text:

February 25, 2026


To: All Transwestern Customers

Subject: Force Majeure - Compressor Station P3

Reason: Mechanical Failure

Revision 1 - This Force Majeure Event has been edited and extended through Thursday 3/5/26. Please see capacity and date change below.

Gas Day February 22, 2026 (Intraday 3) through February 25 (Evening Cycle), 2026

P-3 Station Delivery Capacity reduced from 253,000 MMBtu/d to approximately 180,000 MMBtu/d. (Original reduction was 180,000)

We anticipate this will impact approximately 40,000 MMBtu/d of scheduled volumes.

Gas Day February 25, 2026 (Intraday 1) through March 5, 2026

P-3 Station Delivery Capacity increased from 180,000 MMBtu/d to approximately 190,000 MMBtu/d.

We anticipate this will impact approximately 30,000 MMBtu/d of scheduled volumes.

Interconnects Affected:
POI 57274 -ANR Red Deer
POI   9198 - CIG Tumbleweed
POI 79064- Enbridge Trunk E (Palo Duro)
POI   8042 - PEPL Hansford/Sherman
POI 60667 - NNG Gray
POI 10594 - Southern Star

March 6, 2026

Back to full capacity through P-3 Compressor Station.


Reason:
Notice Type Description: Force Majeure
Notice Identifier: 115365
Critical Notice Description: Critical notice
Posting Date/Time: Feb 25 2026 9:30AM
Notice Status Description: Supersede
Required Response Indicator Description: No response required
Response Date/Time:
TSP: 7933047
TSP Name: TRANSWESTERN PIPELINE COMPANY, LLC
Subject: Force Majeure - Compressor Station P3 - 2/22/2026 (Intraday 3) through 3/05/2026 Revision 1
Notice Effective Date/Time: Feb 22 2026 4:50PM
Notice End Date/Time: Mar 6 2026 8:59AM
Notice Text:

February 25, 2026


To: All Transwestern Customers

Subject: Force Majeure - Compressor Station P3

Reason: Mechanical Failure

Revision 1 - This Force Majeure Event has been edited and extended through Thursday 3/5/26. Please see capacity and date change below.

Gas Day February 22, 2026 (Intraday 3) through February 25 (Evening Cycle), 2026

P-3 Station Delivery Capacity reduced from 253,000 MMBtu/d to approximately 180,000 MMBtu/d. (Original reduction was 180,000)

We anticipate this will impact approximately 40,000 MMBtu/d of scheduled volumes.

Gas Day February 25, 2026 (Intraday 1) through March 5, 2026

P-3 Station Delivery Capacity increased from 180,000 MMBtu/d to approximately 190,000 MMBtu/d.

We anticipate this will impact approximately 30,000 MMBtu/d of scheduled volumes.

Interconnects Affected:
POI 57274 -ANR Red Deer
POI   9198 - CIG Tumbleweed
POI 79064- Enbridge Trunk E (Palo Duro)
POI   8042 - PEPL Hansford/Sherman
POI 60667 - NNG Gray
POI 10594 - Southern Star

March 6, 2026

Back to full capacity through P-3 Compressor Station.


Reason: