Transco Pipeline Notice 16987620
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| Critical: | Y |
| Notice Eff Date: | 06/23/2026 |
| Notice Eff Time: | 10:41:27 CDT |
| Notice End Date: | |
| Notice End Time: | |
| Notice ID: | 16987620 |
| Notice Stat Desc: | Initiate |
| Notice Type Desc: | Maint |
| Post Date: | 06/23/2026 |
| Post Time: | 10:41:27 CDT |
| Prior Notice: | 0 |
| Reqrd Rsp Desc: | Immediate response required of an operational nature may be required of impacted shippers |
| Rsp Date: | |
| Rsp Time: | |
| TSP: | 007933021 |
| TSP Name: | TRANSCONTINENTAL GAS PIPE LINE COMPANY, LLC |
Notice Text:
Subject: Unplanned Maintenance Station 50 Compressor Outage
Due to an equipment failure on Main Unit 9 at Station 50, Transco must immediately restrict scheduled quantities moving south to north through the TSB below. The constraint will be effective ID1, 6/23/2026. The duration of this outage is anticipated to be 1 day.
The receipt-based Throughput Section Boundary (TSB) at mainline MP 517 (Station 50) will be used to manage capacity availability during this outage. An updated Market and Production Area constraint notice will include the location and the available quantity of all transportation services during the indicated period.
|
TSB Name Location |
Location ID |
Flow Direction |
|
COMPRESSOR STATION W 50 MP 517.23 |
9013363 |
South to North |
|
Estimated Outage |
Design Capacity (Mdt/d) |
Total Qty Available (Mdt/d) |
% Available Total Primary-Firm vs Design Capacity |
% Cuts (Primary)Potential Shipper Impact (Based on Historical Utilization) |
|
June 23, 2026 |
1,536 |
1,420 |
92% |
5-10% |
If you have any questions, please contact your Transportation Services Representative.