AMENDED: Unplanned Service Outage - Flow South of Cushing CS #2213
Viking Gas Transmission Company 6d ago
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TSP Name: Viking Gas Transmission Company
TSP: 60-916-6673
Subject: AMENDED: Unplanned Service Outage - Flow South of Cushing CS #2213
Notice Type: Constraint
Critical: Yes
Post Date/Time:: 10/31/2025 01:33 pm
Notice Eff Date/Time: 10/31/2025 09:00 am
NOTICE_END_DATE: 11/16/2025 09:00 am
Notice ID: 3165
Notice Stat Desc: Supersede
Prior Notice: 3157
Reqrd Rsp Desc: No response required
Rsp Date/Time:
Notice Text:
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will amend the capacity constraint as follows:
Effective Gas Day Tuesday, November 4, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will decrease from 410,852 Dths to 391,217 Dths. The capacity will remain at 391,217 Dths through Gas Day Friday, November 7, 2025, ID3.
Effective Gas Day Saturday, November 8, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will increase from 391,217 Dths to 419,954 Dths. The capacity will remain at 419,954 Dths through Gas Day Friday, November 14, 2025, ID3.
Effective Gas Day Saturday, November 15, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will be reinstated to 429,218 Dths.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3160
The unplanned service dates for Viking Gas Transmission Company (VGT) maintenance at the Cushing Compressor Station (CS) #2213 have been amended. The new unplanned service outage will begin Gas Day Tuesday, November 4, 2025, Timely Cycle, and is anticipated to be in effect through Gas Day Friday, November 14, 2025.
For more details, please refer to the posting below (Prior Notice ID 3157). This posting will be updated with any changes.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3157
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will decrease the flow South of Cushing CS #2213 capacity beginning Gas Day, Friday, October 31, 2025, Timely Cycle. This capacity constraint is anticipated to be in effect through Gas Day, Saturday, November 8, 2025, Evening Cycle.
Flow South of Cushing CS #2213 capacity will be reduced from 429,218 Dth to 410,852 Dth.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.
TSP: 60-916-6673
Subject: AMENDED: Unplanned Service Outage - Flow South of Cushing CS #2213
Notice Type: Constraint
Critical: Yes
Post Date/Time:: 10/31/2025 01:33 pm
Notice Eff Date/Time: 10/31/2025 09:00 am
NOTICE_END_DATE: 11/16/2025 09:00 am
Notice ID: 3165
Notice Stat Desc: Supersede
Prior Notice: 3157
Reqrd Rsp Desc: No response required
Rsp Date/Time:
Notice Text:
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will amend the capacity constraint as follows:
Effective Gas Day Tuesday, November 4, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will decrease from 410,852 Dths to 391,217 Dths. The capacity will remain at 391,217 Dths through Gas Day Friday, November 7, 2025, ID3.
Effective Gas Day Saturday, November 8, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will increase from 391,217 Dths to 419,954 Dths. The capacity will remain at 419,954 Dths through Gas Day Friday, November 14, 2025, ID3.
Effective Gas Day Saturday, November 15, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will be reinstated to 429,218 Dths.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3160
The unplanned service dates for Viking Gas Transmission Company (VGT) maintenance at the Cushing Compressor Station (CS) #2213 have been amended. The new unplanned service outage will begin Gas Day Tuesday, November 4, 2025, Timely Cycle, and is anticipated to be in effect through Gas Day Friday, November 14, 2025.
For more details, please refer to the posting below (Prior Notice ID 3157). This posting will be updated with any changes.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3157
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will decrease the flow South of Cushing CS #2213 capacity beginning Gas Day, Friday, October 31, 2025, Timely Cycle. This capacity constraint is anticipated to be in effect through Gas Day, Saturday, November 8, 2025, Evening Cycle.
Flow South of Cushing CS #2213 capacity will be reduced from 429,218 Dth to 410,852 Dth.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.
TSP Name: Viking Gas Transmission Company
TSP: 60-916-6673
Subject: AMENDED: Unplanned Service Outage - Flow South of Cushing CS #2213
Notice Type: Constraint
Critical: Yes
Post Date/Time:: 10/31/2025 01:33 pm
Notice Eff Date/Time: 10/31/2025 09:00 am
NOTICE_END_DATE: 11/16/2025 09:00 am
Notice ID: 3165
Notice Stat Desc: Supersede
Prior Notice: 3157
Reqrd Rsp Desc: No response required
Rsp Date/Time:
Notice Text:
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will amend the capacity constraint as follows:
Effective Gas Day Tuesday, November 4, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will decrease from 410,852 Dths to 391,217 Dths. The capacity will remain at 391,217 Dths through Gas Day Friday, November 7, 2025, ID3.
Effective Gas Day Saturday, November 8, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will increase from 391,217 Dths to 419,954 Dths. The capacity will remain at 419,954 Dths through Gas Day Friday, November 14, 2025, ID3.
Effective Gas Day Saturday, November 15, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will be reinstated to 429,218 Dths.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3160
The unplanned service dates for Viking Gas Transmission Company (VGT) maintenance at the Cushing Compressor Station (CS) #2213 have been amended. The new unplanned service outage will begin Gas Day Tuesday, November 4, 2025, Timely Cycle, and is anticipated to be in effect through Gas Day Friday, November 14, 2025.
For more details, please refer to the posting below (Prior Notice ID 3157). This posting will be updated with any changes.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3157
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will decrease the flow South of Cushing CS #2213 capacity beginning Gas Day, Friday, October 31, 2025, Timely Cycle. This capacity constraint is anticipated to be in effect through Gas Day, Saturday, November 8, 2025, Evening Cycle.
Flow South of Cushing CS #2213 capacity will be reduced from 429,218 Dth to 410,852 Dth.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.
TSP: 60-916-6673
Subject: AMENDED: Unplanned Service Outage - Flow South of Cushing CS #2213
Notice Type: Constraint
Critical: Yes
Post Date/Time:: 10/31/2025 01:33 pm
Notice Eff Date/Time: 10/31/2025 09:00 am
NOTICE_END_DATE: 11/16/2025 09:00 am
Notice ID: 3165
Notice Stat Desc: Supersede
Prior Notice: 3157
Reqrd Rsp Desc: No response required
Rsp Date/Time:
Notice Text:
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will amend the capacity constraint as follows:
Effective Gas Day Tuesday, November 4, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will decrease from 410,852 Dths to 391,217 Dths. The capacity will remain at 391,217 Dths through Gas Day Friday, November 7, 2025, ID3.
Effective Gas Day Saturday, November 8, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will increase from 391,217 Dths to 419,954 Dths. The capacity will remain at 419,954 Dths through Gas Day Friday, November 14, 2025, ID3.
Effective Gas Day Saturday, November 15, 2025, Timely cycle, Flow South of Cushing CS #2213 capacity will be reinstated to 429,218 Dths.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3160
The unplanned service dates for Viking Gas Transmission Company (VGT) maintenance at the Cushing Compressor Station (CS) #2213 have been amended. The new unplanned service outage will begin Gas Day Tuesday, November 4, 2025, Timely Cycle, and is anticipated to be in effect through Gas Day Friday, November 14, 2025.
For more details, please refer to the posting below (Prior Notice ID 3157). This posting will be updated with any changes.
Please contact your Commercial representative with questions.
-------------------------------------------
Prior Notice ID: 3157
Due to unplanned maintenance at the Cushing Compressor Station (CS) #2213, Viking Gas Transmission Company (VGT) will decrease the flow South of Cushing CS #2213 capacity beginning Gas Day, Friday, October 31, 2025, Timely Cycle. This capacity constraint is anticipated to be in effect through Gas Day, Saturday, November 8, 2025, Evening Cycle.
Flow South of Cushing CS #2213 capacity will be reduced from 429,218 Dth to 410,852 Dth.
VGT does anticipate an impact to firm transportation service. Reservation charge credits will be applied pursuant to VGT's FERC Gas Tariff, General Terms and Conditions, Section 34.
Please contact your Commercial representative with questions.